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  • Putting Tire Sealant in Presta Valve Tubes

    Posted on October 15th, 2009 Lee Devlin 2 comments

    I got a new bike earlier this summer (a Kona Dew Deluxe) and it’s a sort of cross between a mountain bike and a road bike. It uses the narrow 700 cm road tires and so I’m learning to deal with Presta valves whenever I need to inflate the tires. That requires putting an adapter on the valve stem since my air compressor is set up for much more common Schrader valves.
    kona-dew-deluxe
    One of the annoyances of bicycling on the Front Range of Colorado is the abundance of thorns called ‘goat heads‘. They will easily puncture bicycle tires. I learned this many years ago when I purchased my first bike in Colorado only to get two flats tires on the same day I took it for its first spin. When I returned to the bike shop, they asked if I had put TR tubes in it yet. TR tubes? “What are those and why didn’t you let me know about this when I bought the bike?” I was new to Colorado and never heard of TR tubes. “TR” stands for thorn resistant and their outside wall is about 4 times thicker than that of standard tubes and so the goat heads generally cannot penetrate in far into the tube wall enough to puncture it. After installing these tubes, I didn’t have any more problems with flat tires from the goat heads on my mountain bike.

    However, with my new bike, despite putting TR tubes in it before leaving the bike shop, I’ve had several flats from goat heads. I guess it’s because the rubber on both the tire and the tube is thinner to begin with than standard 26″ mountain bike tires. So I needed another plan. I see a lot of Slime tube sealant for sale these days in bike shops, and I was wondering if there would be a way to get it into tubes that had these newfangled Presta valves since the cores didn’t appear to be removable. I looked on the Internet and found several websites that talked about a method of using cutters to clip off the last few threads on the part that holds on the nut you need to loosen to put air in Presta valves. This causes the threaded part to fall into the tube which allows enough room to put the Slime in the tire. Then you have to push the threaded part back up into the stem and secure it with the nut, which now has no locking thread to keep you from unscrewing it all the way. I was hoping that I would not have to do that. I found that I was in luck because my tubes had Presta valves that allowed me to remove their cores. If you look at the part of the valve that has the threads to hold the valve cap on and it has flats on it, then that means the core can be unscrewed.

    presta-valve-1

    This Presta valve above has flats on the threaded part that holds on the cap which means the core can be unscrewed from the valve stem.

    presta-valve-2

    presta-valve-3

    In my case, I already had some Slime but my local bike shop guy, Mark at International Bike in Greeley, is a strong proponent of True Goo. He believes that this product is easier than Slime to put in the tire due to its lower viscosity and that it seals better too.

    If you search on the Internet, you’ll see a lot of people telling you these tube sealants don’t work. I think the reason for this is that it’s still possible to get a flat even with tube sealant, especially if the hole is so big that the sealant comes out so fast it can’t solidify. Also, people are much more likely to post a rant about a product that let them down rather than to take the time to post a positive review. In addition, when tire sealant works, you don’t really have hard evidence to let you know that you would have gotten a flat if you didn’t have the sealant in the tube. So it’s hard to measure tube sealant’s effectiveness.

    In my case, I had the perfect experiment. My rear tire’s tube was losing nearly all its air every 2 days. It meant that each time I wanted to go for a ride, I needed to put air in the tire. I had debated on whether to patch or replace the tube, but then I realized that it would be a great experiment to see for myself whether tire sealant actually works, especially on slow leaks, which are the kind you generally get from the tiny holes that goat heads put in the tubes.

    In order to put the sealant in the tire, my bicycle guy gave me some good advice. The rubber transfer tube that comes with these sealants is sized to be a press-fit on Shrader valves, which is much too large in diameter to seal on Presta valve stems. However, if you gradually cut the top of the cone-shaped nozzle until it is a press-fit for a .22 caliber cartridge, it will also be a press fit on a Presta valve which is about .235″ in diameter. You can also use the .22 bullet as a cap because the red cap that is included with it will no longer fit after you cut that much of the tip off the nozzle. You can use a spent .22 caliber casing or something else that is similar in diameter if you’re worried about using live ammunition to seal the bottle. Here’s a picture of what it looks like:

    True Goo tire sealant

    True Goo tire sealant

    If your Presta valve has a removable core, you can even put the sealant in when the tire is on the bike. Just rotate the valve to the top, insert the nozzle on the valve stem, and rotate it back around to the bottom. Squeeze in about 3 ounces of fluid, rotate back to the top, remove the bottle. Then replace the valve core and fill it with air.

    I found that my tire that leaked down every 2 days consistently has now held its pressure for several weeks, which leads me to believe that this stuff actually works as advertised.

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  • Replacing Remington and Norelco Shaver Batteries

    Posted on April 6th, 2008 Lee Devlin 48 comments

    I have a feeling this will be one of those blog entries that will generate a long tail of hits.

    I came to the realization that I’ve never worn out a Norelco or Remington razor yet I’ve owned a number of them over the years. But I have worn out a number of shaver batteries. My first Norelco razor was a plug-in only model. I was lured into buying a battery-powered model that would let me shave without being tethered to the wall outlet. Over the course of a year or so, I noticed that the charge on the battery wasn’t lasting very long and so this eventually became no different than the model that had to be connected to the AC outlet all the time. I bought a replacement when I was planning a camping trip and would not have dependable access to an AC outlet. Over the course of a few years, this model did the same thing, i.e., its batteries wore out and it also had to be plugged in all the time.

    At the time, I priced a service that would replace the batteries and figured out, like many others, I’m sure, that it wasn’t much more expensive to buy a new razor than to repair an old one. So I opted to get a Remington R9190 model that I could clean by running it under the water tap. What would they think of next? It had amazing capacity, providing 60 minutes of shaving on a single charge. However, after about 18 months, it too, needed to be left plugged in all the time.

    I figured that these razors only needed new batteries, but knew that it would require getting the right kind of batteries, and then having to do some unsoldering and re-soldering. I found a website that sold shaver batteries and would provide the correct ones for the razors based on their model numbers. In this case, the razor model numbers I wanted to fix were a Norelco 6843XL and a Remington R9190. I found the battery packs at Electricshaver.com. In the case of the 6843XL, I received a single AA 600 mah NiCad battery with solder tabs at a cost of $9.95. The R9190 battery pack contained a pair of AA NiCads with solder tabs that were joined together at one end. I had to cut these apart to actually install them so it probably would have been better if they just provided two AA solder tab batteries. That battery pack cost $14.95. I realized afterwards that I could probably just have just ordered 3 regular solder tab AA NiCad batteries from any of a number of Internet sources for around $3.00 each and saved about $15. Live and learn.

    The Norelco 6843XL came apart quite easily. I just removed two screws (although I did need to use a torx driver) and then popped its snap joints apart. The battery tabs of the single AA battery were soldered through the PC board, but with a solder sucker and some solder wick, they were easily removed and the battery was replaced.

    The Norelco 6843XL was easy to take apart. It contained a single AA solder-tab battery.

    The R9190 wasn’t as easy to disassemble. There were 4 exposed phillips head screws which I removed, but the casing still would not come apart. After a lot of time fiddling, I found that there were two more hidden screws under the rubber backing and once these were removed, everything came apart. It was first necessary to pry up the corners of the rubber backing which was glued down on the back of the shaver (as shown in the photo) to expose the hidden screws. I came close to giving up on it. It’s the reason you may have found this posting, because searching for ‘Remington R9100 R9190 R9200 shaver battery replacement’ came up with nothing on the Internet. So I figure that within a few weeks of posting this, it will start to get hits because if I’m having this problem, chances are pretty good that others are as well.

    The R9190 had two hidden screws keeping it together. After prying up the rubber as shown in the photo, the screws were exposed.

    The main reason I’m posting this is because I know how much I appreciate it when I find some obscure piece of information on the Internet that allows me to fix something that I’d otherwise have to throw away. I’m disappointed that Norelco and Remington continue to build products whose batteries cannot be easily serviced. I’ve read recently that many cellphones get replaced when their batteries goes bad after around 18 months of use. I find that to be extremely wasteful, and in the case of most cellphones, completely unnecessary because the batteries are generally easily replaced (unless you have an iPhone) . Of course, the battery packs sometimes have excessive markups on them when purchased from the manufacturer so that probably contributes to it as well.

    I think that building batteries into a product in such a way that they cannot be replaced by an end user is unacceptable. Rechargeable batteries are only good for around 500 charge cycles and then they must be replaced. I wouldn’t want to be associated with a product where the batteries are so difficult to replace that the battery life determines the useful life of the product.

    The R9190 has two AA NiCad batteries soldered together with some wiring. They are relatively easy to replace once you figure out how to get the case apart.

    Both shavers are working great now and I can again enjoy the experience of untethered shaving.

    UPDATE 2009-01-25

    I continue to get a lot of hits on this web page so I can only imagine that many people have encountered the same problem, i.e., a razor that is still working, but with batteries that have gone flat. A very nice gentleman sent me the images below complete with annotations to show how he repaired his Remington Model 8100 razor. He replaced the solder tail AA batteries with holders for AAA batteries. Even though AAA batteries are much smaller, and usually have half the capacity of AA batteries, he found some that had nearly equal capacity to the AA batteries he replaced. The best part of his repair is that the next time they go flat, it will be very easy to replace them because it will require no soldering.

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  • PC Resuscitation

    Posted on December 5th, 2007 Lee Devlin 1 comment

    I get a lot more satisfaction out of fixing things than I do replacing them. Part of it is the challenge, part of it is the learning experience, and part of it is the savings. But I think the biggest part of it may be genetically programmed into my DNA.

    I do realize that sometimes it’s cheaper to replace something than it is the repair it. The other day I was looking over a broken electric can opener that we had replaced for the princely sum of $15 and realized that it was not worth repairing. I didn’t know what I’d do with an extra used electric can opener if I did repair it when they are available new for as little as $6 at Target.

    I got an inquiry last week from my cousin in Pennsylvania about whether a power supply for a Compaq PC manufactured in 2002 should cost $185. I am usually able to pick up PC power supplies for as little $15 to $25, and so this price seemed way out of line. Upon further investigation I found that back in 2002 Compaq was using a non-standard connector and case size in their desktop power supplies. This makes the power supply rare and therefore very expensive. After looking over the pinout of the motherboard connector for the Presario 5000 model, it appeared that the majority of the pins were consistent with the ATX standard, but there were enough changes that it would take some fiddling to adapt a standard power supply to work like the Compaq model. The failure mode didn’t seem consistent with a normal power supply failure though. Usually when a PC’s power supply fails, the computer will show no signs of life. In this case, the computer would power on, but in a short time would shut itself down. This made me suspect that perhaps there was a bad electrolytic cap on the motherboard that would short and cause an over-current condition after things warmed up. If that were true, even a new power supply wouldn’t fix the problem.

    My uncle is quite handy designing and fixing all things electrical and mechanical and offered to help. Despite having very little experience with computers, in a relatively short time, he and another relative were able to determine that the power supply’s fan had stopped spinning. That would explain why it was powering on but shutting down after a while. He went to Radio Shack and found a similar fan but it would not fit inside the power supply’s case. No problem, he mounted it outside the computer’s case over the power supply vent. It still fulfills the need of moving air through the power supply to prevent it from overheating. The fix worked and the PC has been successfully resuscitated.

    It may be his nearly 70 years of ham radio and tinkering experience that came to the rescue because once you understand how things work, you can fix them even if you’ve never done a repair exactly like it before.

    And then, of course, there’s that DNA thing too.

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  • Zen and the art of deck repair

    Posted on November 18th, 2007 Lee Devlin 1 comment

    Lately I’ve been trying work on my Zen habits and one of the tenets of this philosophy is to get rid of things that you are no longer using. An item in our lives that added cost and complexity and was no longer providing equivalent value was our hot tub. It came with the house and we used it for a while, but got out of the habit after a few years. It just continued to require energy, chemicals, and periodic repair that was out of proportion to the value we were getting from it. So we decided to give it away. I removed the decking surrounding it and with the help of a sawsall and eventually a chainsaw, I eventually liberated the deck structure that had been built around it. An ad for a functioning free hot tub on Craigslist resulted in 9 eager takers in less than 4 hours. Two people arrived for it around the same time and after a coin toss, the tub had a new owner. I wrote up a blog entry about it in July.

    If you’re ever considering whether you should put a hot tub on top of your deck or build it into your deck, please choose on top of the deck. You’ll be much better off in the long run. Hot tubs require maintenance and building the tub into a deck makes maintenance much more difficult.

    So for a few months, the gaping hole in the deck stared at me and I stared back at it wondering what would be the best way to fill it in. We joked about putting in a fish pond to entertain the cat and quickly realized that it would contain water and pumps and probably be a bigger maintenance headache than a hot tub. Thus it would definitely not be aligned with my desire to be more zen-like.

    After removing the hot tub I soon realized that the deck had an oddity to it that wasn’t apparent prior to the tub’s removal. The main joists where the decking met were not aligned on the opposite sides of the hot tub. I wondered if this would present a problem if I were to have visible mismatch where the joists met in the middle or if it might look artsy. I drew it up in Autocad and realized that it would be very strange looking as you can see in the image below.

    I decided I probably had to do some more surgery on the deck to get the main joists in alignment. After making another drawing, this time with the joists meeting at a center, I was much happier with the result. I removed the misaligned joists so that new ones could be installed that would align with the other joists.

    I had previously met a handyman through Craigslist when I needed some work done on my siding. He was very professional and let me provide a lot of input, buy the materials, and didn’t charge me any extra for my help. I decided to hire him again for the deck work because I knew with some professional help, the job would go very quickly once it got started. A colleague of Terri’s joked that I must have been in the corporate world too long because I was outsourcing my handyman jobs. Maybe, but I know good help when I see it and I’m more than happy to pay for it.

    The hole in the deck left by removing the hot tub.


    I was in charge of the design and the materials. Here we have the pressure treated 2 x 8 joists and the 2 x 6 redwood planks.


    Here are the joists with the redwood decking just starting to be installed. The joists were supported every 2 feet on the concrete pad in case anyone ever wants to put another hot tub on top of the deck. I also left the access door for the electrical wiring in the deck.

    And here it is, all finished and looking like new. As the wood ages the colors will blend in. Right after a pressure washing, all the wood looks new like the new decking in the middle. That will be job for next spring.

    UPDATE 2007-Dec-05:

    We received a pleasant surprise in our electric bill today. It was 40% less than last year’s bill for November. The electricity cost to run a hot tub was one of those things that I never really wanted to contemplate when we owned it. Now that it’s gone, I’m only too happy to know what the savings will be. Based on some web research, a reasonable estimate for hot tub energy consumption appears to be between $400-$600/year and much of that is incurred in the winter when the difference between the outside temperature and the water in the tub is at a maximum. The cost of the chemicals and periodic repair added up too, easily adding a few hundred more per year to the overall cost. So the missing tub is already beginning to pay for the deck repair with negawatts and also by eliminating the cost of chemicals and maintenance.

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  • Removing a hot tub from a deck

    Posted on July 5th, 2007 Lee Devlin 2 comments

    Last weekend Terri asked me to work on finding a new home for our hot tub. The hot tub came with the house that we purchased in 1994. We enjoyed it for a while, but then got out of the habit and thought it would be best to sell it or give it away to someone who would use it. Paying to heat and maintain a hot tub can be expensive, particularly when it needs repairs. Our last repair bill was nearly $800 because it required replacing the heater box, recirculating pump, and some of the tubing. It was also leaking and that was repaired at the same time too.

    I put an ad on Craigslist and attached the picture above letting anyone know that if they wanted the tub, they could have it for free if they moved it themselves. Prior to placing the ad, I had called the hot tub store and asked what it cost to have it professionally moved and they told me it would be around $300-$500 depending on the complexity and about $100/hour for every hour extra they need to spend. They also told me the model of hot tub I had weighed about 900 lbs. In about 4 hours after placing the ad for a free hot tub, I had 9 responses from interested parties. That evening a guy stopped by to look at it and while he was here another guy showed up also wanting to take the tub. I suggested a coin toss to which they both agreed and that resulted in a winner. The coin toss winner said he’d come back with some friends and equipment to retrieve the tub a few days later. I told him I’d work on removing some of the decking to make it accessible.

    The main problem was that the hot tub was built into our redwood deck. Actually, the deck was built around it like a jig saw puzzle because the hot tub was installed on a concrete pad before the deck was built. The floor boards on the deck are attached with long wood screws, so I didn’t anticipate a problem removing them…. until I actually tried to do it. Most of the screws were screwed well below the wood surface, up to a half inch deep in some places, which caused the screw head to disappear below the surface of the deck. This also caused the holes to fill with dirt and wood, so before I could remove most of the screws, I had to first excavate them. I used a drill with a Forstner bit to remove the wood above them, then an exacto knife to clean out the dirt in the screw heads and then a right angle screw driver to provide enough leverage and get them started so that I didn’t strip out the heads. It took me a good 5 hours working in the heat to get enough boards out of the deck to find out that a much bigger challenge lay ahead. The hot tub had a massive frame built around it and I would have to remove that frame before the tub could be lifted because we couldn’t get anything under the tub to lift it out with the frame in place. I removed a few more floor boards and then used a Sawzall to cut the joists, which worked for the stringers, but there were a few parts of the frame that required cutting through stringers that had been doubled or tripled, so I pulled out my chainsaw. A chainsaw is an interesting tool to use for working on a beautiful redwood deck. But in a surprisingly short time, I had severed enough joists and members in the frame so that Terri and I could lift the frame away from the hot tub.

    After we got this taken care of, our buyer showed up with 3 friends along with a flat bed trailer and a pair of flat dollies. He was well prepared with various tools, and yet we were still unsure of how we would lift the 900 lb tub up out of the hole it was set down in. One guy suggested we just try to lift it as he had done with his hot tub. I thought that couldn’t hurt as long as we took it easy so between the 5 of us we found that it was in fact possible to lift the tub. We got one end of it up on the deck only to find we forgot to remove the wiring. Oops. We put some wood under the dangling end of the tub while one guy took care of unwiring it. Then we tilted it up on end, on to the dolly, so it would fit out through the gate which was about 4 feet wide. One guy had built a small ramp with bricks and plywood to roll it safely down the one step between the patio and the sidewalk and then we wheeled it out to the flat bed trailer. The whole ordeal took less than 20 minutes and would have take half that had we remembered to unwire it first. It was quite a relief.

    Now the tub is on its way to a new home where it will no doubt see much more use that it had here. And I have a large hole in my deck to fill in.

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  • Rebuilding the electric range

    Posted on April 7th, 2007 Lee Devlin No comments

    A few months ago, I repaired the washing machine and wrote about it in a blog posting. Lately, our stove has been acting up, not heating up its burners until they were ‘wiggled’ a bit. It’s actually been a recurring problem for a while, but was isolated to just one or two elements. Over the past year, it seemed that all of them have been having the same issue at one time or another.

    First I took them out and noticed that the contacts were pretty dirty and so I sanded them down, which seemed to help. But then a few of them quickly became intermittent again. I looked at the price of new burners online and found them to be priced quite high, between $30 to $40 *each*. I also realized the receptacles, which cannot be cleaned, were the the more likely source of poor electrical contact Those parts weren’t too expensive, about $10 each, so I bought a few of them and spliced them in to replace the ones that were very worn out. This helped quite a bit and we had all 4 elements working reliably for the first time in a long time.

    A few months after that I was noticing that a burner wasn’t working, so I attempted to adjust it in the receptacle and when I turned it on, I heard the a very loud pop and saw a very large blue spark jump from the receptacle. I guess that’s what I get for not ‘doing it right the first time’ and just replacing all the receptacles and burners. After that spark, that burner position no longer worked because it evidently took out the switch/temperature controller in the panel. Later, I had an experience where the other small (6″) burner did something similar and this time the spark melted a section of the burner and it came apart near the receptacle. I resigned myself to getting 4 new burners and 2 more new receptacles. I still didn’t realize at the time that I’d need two new switch/temperature controllers too.

    If you price out a range by the sum of its replaceable parts, you’ll quickly realize that it can get expensive in a hurry. I found that the 4 burners and 2 more receptacles added up to over $160 and with a new stove costing around $500-600, it doesn’t make much sense spend a lot of money to fix one that is 17 years old. However, I found that the entire set of burners and receptacles were available in a kit (shown below) for $63 from the repairclinic.com and that put the cost of the repair within reason again. I wished I had seen that kit in the first place and I would not have tried to fix the range a piece at a time.

    It’s really not that hard to work on our range because it has a kind of hinge that lets you lift up the front just like a hood on a car. It even has a way to support the top with some wire supports while you work on it. The receptacles were easy to replace and so were the elements. You do have to be careful because it has lethal voltages wired throughout, so you should know where the circuit breaker is for the range and make sure to turn power off to the range when you’re about to touch anything that is electrical.

    After I got the burners and receptacles replaced, I learned that the big blue sparks had taken out two of the switch/temperature controllers because I only measure 40 VAC (instead of 240 VAC) across their output so I had to replace two of those too. These parts were not very attractively priced on-line anywhere I looked, so I ordered them from the local appliance store and got them for about 30% less than the on-line price even taking tax into consideration.

    Now the range is virtually new again and the pots actually sit flush on the burners which start up immediately with they are turned on. One of the more gratifying things about working on appliances is that you can become a total geek with your tools and multimeter and in the end, it results in a wife who is happy with the result :-) . Very few geek adventures offer that as an incentive.

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  • Whirlpool Washer Transmission Repair

    Posted on January 21st, 2007 Lee Devlin 49 comments

    A few months ago our whirlpool washer wouldn’t spin. It did everything else, but it was pretty worthless without the spin function because the clothes would just be sitting at the bottom of it completely soaked after a wash. Of course, the first thing I did was go to Google and type in “Whirlpool washer won’t spin” and got a lot of hits on some great websites. Most of them were repair websites and forums sponsored by kind individuals who freely share their knowledge such as fixitnow.com. Others are sponsored by companies who sell parts to DIY homeowners, like repairclinic.com.

    The forums always suggest the most common and easy fixes first, like the lid switch, which wasn’t my problem. So I had to start disassembling the washer because the next item on the list was the coupling on the motor. Fortunately, these websites have directions on how to get the washer open, which takes very little effort, as long as you know which screws to remove and in what order. I knew that the coupling was unlikely to be the failed item because the agitator was still working and it would be unlikely that a failed coupling would allow that to work. Then I started looking at the clutch/brake mechanism and that also looked OK. Finally, I figured it had to be the transmission, one of the hardest items to remove. I had the entire washer torn apart and moved to the kitchen because our laundry room is more of an alcove in the entryway between the garage and the kitchen.

    After pulling the transmission, I was faced with the prospect of taking it apart, knowing it would be filled with heavy oil.

    To pull your washer’s transmission, you need to remove a bolt at the top of the shaft holding it to the agitator. You have to pull off the plastic cap on the top of agitator as well as another translucent seal below it to gain access to the bolt. Note the translucent cap has an o-ring seal on it. Make sure to put it back in properly when you re-assemble the washer to keep water out of that bolt’s compartment or it will rust and fuse with the shaft.

    I carefully took out all the screws holding on the transmission’s top cover and drained the oil into a jar. This was going to a really messy job and so I put on some vinyl mechanics gloves.

    Whirlpool Transmission

    I was amazed at the complexity of the transmission. It has to perform several functions, all without any input other than the direction and speed of the motor. For instance, it has to agitate, spin, and also go into neutral without any shifters or solenoids. The same motor is simultaneously running the pump from a portion of the drive shaft that comes out the other end. The transmission uses a rather complex plate of pawls, gears, and cams on something called the ‘rack retainer’. I was trying to simulate spinning the motor forward and backward and thus I could shift it from spin mode to agitate mode, but I couldn’t get it into spin. It was then that I realized that something called a ‘shoulder pawl stud’ was broken off at its threads and the rack retainer was spinning freely. This pawl stud works as an axle and also as a way of getting the plate to spin along with the spin gear, but it was broken with its threads embedded in the main gear. So I had to find a new pawl stud and figure out a way to extract the threads from the hole they were in. I was pretty sure that the threads had some locking compound on them and they weren’t going to come out easily.

    Whirlpool Transmission

    The pawl stud wasn’t available as a separate part, but there was something called the Neutral Drain Pack from Repairclinic.com which included a lot of parts, including 2 different studs, since Whirlpool evidently beefed up the threads for the newer models, no doubt because it was a weak point. The upside to that is that if I ruined the threads extracting the broken stud, I could drill and tap it for the larger stud and newer rack retainer. So as Terri headed off to the laundry mat, I order the parts on line. The neutral drain kit was about $17 + $6 shipping. In the meantime, I tried to drill the screw threads out of the main drive gear. I broke a drill bit doing it, but got enough of a hole down through the middle of the broken screw shaft that I thought I’d have success with an ‘easy out’. I took it into work and borrowed an easy out and with the help of an arbor press to apply pressure to the easy out, I extracted the broken screw without doing any damage to the threads.

    A few days later, the parts arrived. The kit contained a lot more parts than I needed. I replaced all the old parts with new ones, figuring after 15 years of service, there was no point in reassembling things with old parts when I had new ones right there. Getting everything back together required some head scratching, but after thinking it through, I was able to manually operate the transmission and check the agitate and neutral modes.

    After a little fiddling everything went back together and I ran a cycle through without clothes and was very happy when the spin mode began working again. Now it’s been working for a few months years, I figured that the $23 and my time was worth it because if I had a repairman do it, I’m sure it would have been over $300 because he would have likely replaced the whole transmission. That would be beyond the value of the washer. It was also better than throwing it away and buying a new one for somewhere between $600-900. I generally don’t fix things myself just for the savings because if you consider my time, it’s not really saving me that much. I do it more for the educational experience and the satisfaction of knowing that if it ever breaks again, I can choose to either fix it myself or buy a new one, if we think it’s time for its retirement.

    I’ve included the meager set of instructions for the Neutral Drain Pack in pdf format here.

    UPDATE: 2009-01-07 I continue to get comments and emails on this posting. I just got one asking about getting the transmission apart and so I’ve uploaded a new picture that shows what a messy job this is. Click on it for a higher resolution image.

    The snap ring (shown next to the screw driver laying on the newspaper) needs to be removed from the shaft to get the top cover off of it. I can’t recall if I had the proper snap ring pliers or if I used needle nose pliers ‘in reverse’ to spread open the snap ring by its holes. I managed to save all the oil and reuse it afterward, but if you lose some or it looks dirty you can get more from an appliance service center or use SAE 90 weight gear oil if you can’t find a service center.

    There is also the possibility that your washer is caked with mud, so if the basket won’t spin, it may be clutch that is worn or can’t overcome the friction of mud caked between the basket and the tub like the image below:

    washermud1

    This photo was sent to me by a reader who found mud stuck between the basket and tub. His washer wouldn’t spin because the clutch couldn’t overcome the friction caused by the mud. If your spin cycle is intermittent, then this could be the potential cause of it.

    Another resource you may find useful if you’ve gotten this far is the .pdf file for the service manual for a Whirlpool direct drive washer.

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