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  • Zen and the art of deck repair

    Posted on November 18th, 2007 Lee Devlin 1 comment

    Lately I’ve been trying work on my Zen habits and one of the tenets of this philosophy is to get rid of things that you are no longer using. An item in our lives that added cost and complexity and was no longer providing equivalent value was our hot tub. It came with the house and we used it for a while, but got out of the habit after a few years. It just continued to require energy, chemicals, and periodic repair that was out of proportion to the value we were getting from it. So we decided to give it away. I removed the decking surrounding it and with the help of a sawsall and eventually a chainsaw, I eventually liberated the deck structure that had been built around it. An ad for a functioning free hot tub on Craigslist resulted in 9 eager takers in less than 4 hours. Two people arrived for it around the same time and after a coin toss, the tub had a new owner. I wrote up a blog entry about it in July.

    If you’re ever considering whether you should put a hot tub on top of your deck or build it into your deck, please choose on top of the deck. You’ll be much better off in the long run. Hot tubs require maintenance and building the tub into a deck makes maintenance much more difficult.

    So for a few months, the gaping hole in the deck stared at me and I stared back at it wondering what would be the best way to fill it in. We joked about putting in a fish pond to entertain the cat and quickly realized that it would contain water and pumps and probably be a bigger maintenance headache than a hot tub. Thus it would definitely not be aligned with my desire to be more zen-like.

    After removing the hot tub I soon realized that the deck had an oddity to it that wasn’t apparent prior to the tub’s removal. The main joists where the decking met were not aligned on the opposite sides of the hot tub. I wondered if this would present a problem if I were to have visible mismatch where the joists met in the middle or if it might look artsy. I drew it up in Autocad and realized that it would be very strange looking as you can see in the image below.

    I decided I probably had to do some more surgery on the deck to get the main joists in alignment. After making another drawing, this time with the joists meeting at a center, I was much happier with the result. I removed the misaligned joists so that new ones could be installed that would align with the other joists.

    I had previously met a handyman through Craigslist when I needed some work done on my siding. He was very professional and let me provide a lot of input, buy the materials, and didn’t charge me any extra for my help. I decided to hire him again for the deck work because I knew with some professional help, the job would go very quickly once it got started. A colleague of Terri’s joked that I must have been in the corporate world too long because I was outsourcing my handyman jobs. Maybe, but I know good help when I see it and I’m more than happy to pay for it.

    The hole in the deck left by removing the hot tub.


    I was in charge of the design and the materials. Here we have the pressure treated 2 x 8 joists and the 2 x 6 redwood planks.


    Here are the joists with the redwood decking just starting to be installed. The joists were supported every 2 feet on the concrete pad in case anyone ever wants to put another hot tub on top of the deck. I also left the access door for the electrical wiring in the deck.

    And here it is, all finished and looking like new. As the wood ages the colors will blend in. Right after a pressure washing, all the wood looks new like the new decking in the middle. That will be job for next spring.

    UPDATE 2007-Dec-05:

    We received a pleasant surprise in our electric bill today. It was 40% less than last year’s bill for November. The electricity cost to run a hot tub was one of those things that I never really wanted to contemplate when we owned it. Now that it’s gone, I’m only too happy to know what the savings will be. Based on some web research, a reasonable estimate for hot tub energy consumption appears to be between $400-$600/year and much of that is incurred in the winter when the difference between the outside temperature and the water in the tub is at a maximum. The cost of the chemicals and periodic repair added up too, easily adding a few hundred more per year to the overall cost. So the missing tub is already beginning to pay for the deck repair with negawatts and also by eliminating the cost of chemicals and maintenance.

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  • Removing a hot tub from a deck

    Posted on July 5th, 2007 Lee Devlin 2 comments

    Last weekend Terri asked me to work on finding a new home for our hot tub. The hot tub came with the house that we purchased in 1994. We enjoyed it for a while, but then got out of the habit and thought it would be best to sell it or give it away to someone who would use it. Paying to heat and maintain a hot tub can be expensive, particularly when it needs repairs. Our last repair bill was nearly $800 because it required replacing the heater box, recirculating pump, and some of the tubing. It was also leaking and that was repaired at the same time too.

    I put an ad on Craigslist and attached the picture above letting anyone know that if they wanted the tub, they could have it for free if they moved it themselves. Prior to placing the ad, I had called the hot tub store and asked what it cost to have it professionally moved and they told me it would be around $300-$500 depending on the complexity and about $100/hour for every hour extra they need to spend. They also told me the model of hot tub I had weighed about 900 lbs. In about 4 hours after placing the ad for a free hot tub, I had 9 responses from interested parties. That evening a guy stopped by to look at it and while he was here another guy showed up also wanting to take the tub. I suggested a coin toss to which they both agreed and that resulted in a winner. The coin toss winner said he’d come back with some friends and equipment to retrieve the tub a few days later. I told him I’d work on removing some of the decking to make it accessible.

    The main problem was that the hot tub was built into our redwood deck. Actually, the deck was built around it like a jig saw puzzle because the hot tub was installed on a concrete pad before the deck was built. The floor boards on the deck are attached with long wood screws, so I didn’t anticipate a problem removing them…. until I actually tried to do it. Most of the screws were screwed well below the wood surface, up to a half inch deep in some places, which caused the screw head to disappear below the surface of the deck. This also caused the holes to fill with dirt and wood, so before I could remove most of the screws, I had to first excavate them. I used a drill with a Forstner bit to remove the wood above them, then an exacto knife to clean out the dirt in the screw heads and then a right angle screw driver to provide enough leverage and get them started so that I didn’t strip out the heads. It took me a good 5 hours working in the heat to get enough boards out of the deck to find out that a much bigger challenge lay ahead. The hot tub had a massive frame built around it and I would have to remove that frame before the tub could be lifted because we couldn’t get anything under the tub to lift it out with the frame in place. I removed a few more floor boards and then used a Sawzall to cut the joists, which worked for the stringers, but there were a few parts of the frame that required cutting through stringers that had been doubled or tripled, so I pulled out my chainsaw. A chainsaw is an interesting tool to use for working on a beautiful redwood deck. But in a surprisingly short time, I had severed enough joists and members in the frame so that Terri and I could lift the frame away from the hot tub.

    After we got this taken care of, our buyer showed up with 3 friends along with a flat bed trailer and a pair of flat dollies. He was well prepared with various tools, and yet we were still unsure of how we would lift the 900 lb tub up out of the hole it was set down in. One guy suggested we just try to lift it as he had done with his hot tub. I thought that couldn’t hurt as long as we took it easy so between the 5 of us we found that it was in fact possible to lift the tub. We got one end of it up on the deck only to find we forgot to remove the wiring. Oops. We put some wood under the dangling end of the tub while one guy took care of unwiring it. Then we tilted it up on end, on to the dolly, so it would fit out through the gate which was about 4 feet wide. One guy had built a small ramp with bricks and plywood to roll it safely down the one step between the patio and the sidewalk and then we wheeled it out to the flat bed trailer. The whole ordeal took less than 20 minutes and would have take half that had we remembered to unwire it first. It was quite a relief.

    Now the tub is on its way to a new home where it will no doubt see much more use that it had here. And I have a large hole in my deck to fill in.

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  • How to fix an elecric range

    Posted on April 7th, 2007 Lee Devlin No comments

    A few months ago, I repaired the washing machine and wrote about it in a blog posting and that article gets a lot of hits. Lately, our stove was acting up, not heating up its burners until they were ‘wiggled’ a bit. It’s actually been a recurring problem for a while, but was isolated to just one or two elements. Over the past year, it seemed that all of them have been having the same issue at one time or another.

    First I took them out and noticed that the contacts were pretty dirty and so I sanded them down, which seemed to help. But then a few of them quickly became intermittent again. I looked at the price of new burners online and found them to be priced quite high, between $30 to $40 *each*. I also realized the receptacles, which cannot be cleaned, were the the more likely source of poor electrical contact. Those parts weren’t too expensive, about $10 each, so I bought a few of them and spliced them in to replace the ones that were very worn out. This helped quite a bit and we had all 4 elements working reliably for the first time in a long time.

    A few months after that I was noticing that a burner wasn’t working, so I attempted to adjust it in the receptacle and when I turned it on, I heard the a very loud pop and saw a very large blue spark jump from the receptacle. I guess that’s what I get for not ‘doing it right the first time’ and just replacing all the receptacles and burners. After that spark, that burner position no longer worked because it evidently took out the switch/temperature controller in the panel. Later, I had an experience where the other small (6″) burner did something similar and this time the spark melted a section of the burner and it came apart near the receptacle. I resigned myself to getting 4 new burners and 2 more new receptacles. I didn’t realize at the time that I’d need two new switch/temperature controllers too.

    If you price out a range by the sum of its replaceable parts, you’ll quickly realize that it can get expensive in a hurry. I found that the 4 burners and 2 more receptacles added up to over $160 and with a new stove costing around $500-600, it doesn’t make much sense spend a lot of money to fix one that is 17 years old. However, I found that the entire set of burners and receptacles were available in a kit (shown below) for $76 from the repairclinic.com and that put the cost of the repair within reason again. I wished I had seen that kit in the first place and I would not have tried to fix the range a piece at a time.

    It’s really not that hard to work on our range because it has a kind of hinge that lets you lift up the front just like a hood on a car. It even has a way to support the top with some wire supports while you work on it. The receptacles were easy to replace and so were the elements. You do have to be careful because it has lethal voltages wired throughout, so you should know where the circuit breaker is for the range and make sure to turn power off to the range when you’re about to touch anything that is electrical.

    After I got the burners and receptacles replaced, I learned that the big blue sparks had taken out two of the switch/temperature controllers because I only measure 40 VAC (instead of 240 VAC) across their output so I had to replace two of those too. These parts were not very attractively priced on-line anywhere I looked, so I ordered them from the local appliance store and got them for about 30% less than the on-line price even taking tax into consideration.

    Now the range is virtually new again and the pots actually sit flush on the burners which start up immediately with they are turned on. One of the more gratifying things about working on appliances is that you can become a total geek with your tools and multimeter and in the end, it results in a wife who is happy with the result :-) . Very few geek adventures offer that as an incentive.

    UPDATE: 2012-04-25 This repair has kept the stove running reliably for more than 5 years, and so I wanted to confirm that the fix saved us the cost of a new range and made it much more convenient to use, because we no longer worry about whether one of the burners was not heating. So if you want a stove that works like new, my recommendations is to just buy the repair kit and replace all of the burners and receptacles at once.

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  • Whirlpool Washer Transmission Repair

    Posted on January 21st, 2007 Lee Devlin 126 comments

    A few months ago our whirlpool washer wouldn’t spin. It did everything else, but it was pretty worthless without the spin function because the clothes would just be sitting at the bottom of it completely soaked after a wash. Of course, the first thing I did was go to Google and type in “Whirlpool washer won’t spin” and got a lot of hits on some great websites. Most of them were repair websites and forums sponsored by kind individuals who freely share their knowledge such as fixitnow.com. Others are sponsored by companies who sell parts to DIY homeowners, like repairclinic.com.

    The forums always suggest the most common and easy fixes first, like the lid switch, which wasn’t my problem. So I had to start disassembling the washer because the next item on the list was the coupling on the motor. Fortunately, these websites have directions on how to get the washer open, which takes very little effort, as long as you know which screws to remove and in what order. I knew that the coupling was unlikely to be the failed item because the agitator was still working and it would be unlikely that a failed coupling would allow that to work. Then I started looking at the clutch/brake mechanism and that also looked OK. Finally, I figured it had to be the transmission, one of the hardest items to remove. I had the entire washer torn apart and moved to the kitchen because our laundry room is more of an alcove in the entryway between the garage and the kitchen.

    After pulling the transmission, I was faced with the prospect of taking it apart, knowing it would be filled with heavy oil.

    To pull your washer’s transmission, you need to remove a bolt at the top of the shaft holding it to the agitator. You have to pull off the plastic cap on the top of agitator as well as another translucent seal below it to gain access to the bolt. Note the translucent cap has an o-ring seal on it. Make sure to put it back in properly when you re-assemble the washer to keep water out of that bolt’s compartment or it will rust and fuse with the shaft.

    I carefully took out all the screws holding on the transmission’s top cover and drained the oil into a jar. This was going to a really messy job and so I put on some vinyl mechanics gloves.

    Whirlpool Transmission

    I was amazed at the complexity of the transmission. It has to perform several functions, all without any input other than the direction and speed of the motor. For instance, it has to agitate, spin, and also go into neutral without any shifters or solenoids. The same motor is simultaneously running the pump from a portion of the drive shaft that comes out the other end. The transmission uses a rather complex plate of pawls, gears, and cams on something called the ‘rack retainer’. I was trying to simulate spinning the motor forward and backward and thus I could shift it from spin mode to agitate mode, but I couldn’t get it into spin. It was then that I realized that something called a ‘shoulder pawl stud’ was broken off at its threads and the rack retainer was spinning freely. This pawl stud works as an axle and also as a way of getting the plate to spin along with the spin gear, but it was broken with its threads embedded in the main gear. So I had to find a new pawl stud and figure out a way to extract the threads from the hole they were in. I was pretty sure that the threads had some locking compound on them and they weren’t going to come out easily.

    Whirlpool Transmission

    The pawl stud wasn’t available as a separate part, but there was something called the Neutral Drain Pack from Repairclinic.com which included a lot of parts, including 2 different studs, since Whirlpool evidently beefed up the threads for the newer models, no doubt because it was a weak point. The upside to that is that if I ruined the threads extracting the broken stud, I could drill and tap it for the larger stud and newer rack retainer. So as Terri headed off to the laundry mat, I order the parts on line. The neutral drain kit was about $17 + $6 shipping. In the meantime, I tried to drill the screw threads out of the main drive gear. I broke a drill bit doing it, but got enough of a hole down through the middle of the broken screw shaft that I thought I’d have success with an ‘easy out’. I took it into work and borrowed an easy out and with the help of an arbor press to apply pressure to the easy out, I extracted the broken screw without doing any damage to the threads.

    A few days later, the parts arrived. The kit contained a lot more parts than I needed. I replaced all the old parts with new ones, figuring after 15 years of service, there was no point in reassembling things with old parts when I had new ones right there. Getting everything back together required some head scratching, but after thinking it through, I was able to manually operate the transmission and check the agitate and neutral modes.

    After a little fiddling everything went back together and I ran a cycle through without clothes and was very happy when the spin mode began working again. Now it’s been working for a few months years, I figured that the $23 and my time was worth it because if I had a repairman do it, I’m sure it would have been over $300 because he would have likely replaced the whole transmission. That would be beyond the value of the washer. It was also better than throwing it away and buying a new one for somewhere between $600-900. I generally don’t fix things myself just for the savings because if you consider my time, it’s not really saving me that much. I do it more for the educational experience and the satisfaction of knowing that if it ever breaks again, I can choose to either fix it myself or buy a new one, if we think it’s time for its retirement.

    I’ve included the meager set of instructions for the Neutral Drain Pack in pdf format here.

    UPDATE: 2009-01-07 I continue to get comments and emails on this posting. I just got one asking about getting the transmission apart and so I’ve uploaded a new picture that shows what a messy job this is. Click on it for a higher resolution image.

    The snap ring (shown next to the screw driver laying on the newspaper) needs to be removed from the shaft to get the top cover off of it. I can’t recall if I had the proper snap ring pliers or if I used needle nose pliers ‘in reverse’ to spread open the snap ring by its holes. I managed to save all the oil and reuse it afterward, but if you lose some or it looks dirty you can get more from an appliance service center or use SAE 90 weight gear oil if you can’t find a service center.

    There is also the possibility that your washer is caked with mud, so if the basket won’t spin, it may be clutch that is worn or can’t overcome the friction of mud caked between the basket and the tub like the image below:

    washermud1

    This photo was sent to me by a reader who found mud stuck between the basket and tub. His washer wouldn’t spin because the clutch couldn’t overcome the friction caused by the mud. If your spin cycle is intermittent, then this could be the potential cause of it.

    Another resource you may find useful if you’ve gotten this far is the .pdf file for the service manual for a Whirlpool direct drive washer.

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